Good new's everyone...!
Alan at GAC Motorsport had my engine back for a full check over and dyno to see why i was having all them issues i spoke about on the other posts.
Turn's out i haad some crap in the fuel bowl in one of the carb's, causing it to plug up the fuel circuit around the RPM range i was having the holding back on power.
It was making the motor only run on 3 cylinders...! :eek:
So with that sorted and a few tweaks the motor made more torque and power than the last set up on the dyno as seen below, I can say i'm very happy and top top work from GAC Motorsport
Not bad numbers for a 2165cc
Also had Alan fit and mod a hex type linkage as my CSP bell crank one was fucking up the carbs on idle when the heads got warm and making one side open more lol. And Gary at GM Bodycraft made the throttle cable part to work the hex type as seen here,