Update.
The heads got some machine work on them and we ended up moving the holes for the tubes to seat in, by making a new chamfer for the PR gasket off center from the original center of the hole. That's the short way to tell the story, but was some hours making it happen.
But now i have no rubbing at all!!! Running tapered alu pushrods on K800 springs.
Have done some low boost tuning and ended up with 307whp, 424nm at 7400rpm max (for now) WITH 14,5 PSI and pump gas.
Can't wait to get some E85 in there and more boost.