fahrvergnugen
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« Reply #30 on: July 27, 2009, 11:12:19 am » |
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Looks cool henri! What turbo you running?
Looks like a Tiki turbo Paul.
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mychatype3
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« Reply #31 on: July 27, 2009, 11:47:45 am » |
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Looks cool henri! What turbo you running?
Looks like a Tiki turbo Paul. Nah.... looks more like a cold `martin` turbo
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1968 fastback "in resto" 1970 Westfalia from the States
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kraftwerk
Newbie
Posts: 35
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« Reply #32 on: July 27, 2009, 15:17:30 pm » |
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how you cooling it?? are you running coolant throught the original places, but with an electric pump(would you gain hp by not using a belt driven waterpump???)?
cheers Lee
Kraftwerk
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tikimadness
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« Reply #33 on: July 27, 2009, 16:39:37 pm » |
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how you cooling it?? are you running coolant throught the original places, but with an electric pump(would you gain hp by not using a belt driven waterpump???)?
cheers Lee
Kraftwerk
Yes Henri uses the original cooling system with an electricpump.I don't know what the reason is for going with an electric pump but I think it is for the hp loss that the belt would cause. Michael
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member of team YAC ; the guys who write history.
GASSER GARAGE a few friends creating history.
NIDGAFWYT
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kraftwerk
Newbie
Posts: 35
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« Reply #34 on: July 27, 2009, 17:10:27 pm » |
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how you cooling it?? are you running coolant throught the original places, but with an electric pump(would you gain hp by not using a belt driven waterpump???)?
cheers Lee
Kraftwerk
Yes Henri uses the original cooling system with an electricpump.I don't know what the reason is for going with an electric pump but I think it is for the hp loss that the belt would cause. Michael Cracking idea, cant believe i never thought of it!!! Its the way to go with mine me thinks!! I know hp gains would be negligable, but every bit helps!! weight savin thread is a good one too, they just dont do one for me!!(19st ;-(..)
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mr horsepower
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« Reply #35 on: August 13, 2009, 21:49:27 pm » |
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So got some time of and worked on the car again ,its a slow process but its lokking like a real car again.
gr Henri
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jamiep_jamiep
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« Reply #36 on: August 14, 2009, 08:33:30 am » |
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I love this car!
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Fasterbrit
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« Reply #37 on: August 14, 2009, 08:47:03 am » |
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It gets my vote, too
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ugly duckling
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« Reply #38 on: August 15, 2009, 05:08:18 am » |
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would have rather seen the (REAL BLOWER) go on the engine oh well. good luck with your project. . UD.
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mr horsepower
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« Reply #39 on: August 15, 2009, 07:20:13 am » |
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Hello UD the real blower is getting modified on the moment this setup is so we can race on das drag day 2009 maybe nex year the blower.
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mr horsepower
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« Reply #40 on: August 16, 2009, 17:58:34 pm » |
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« Last Edit: August 16, 2009, 18:01:36 pm by mr horsepower »
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kraftwerk
Newbie
Posts: 35
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« Reply #41 on: August 16, 2009, 18:17:53 pm » |
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nice to see those safety boots on in the workshop environment!!;-)
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kraftwerk
Newbie
Posts: 35
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« Reply #42 on: August 16, 2009, 18:19:10 pm » |
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forgot to say...sounds wicked!! well done!!
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Black Sheep
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« Reply #43 on: August 16, 2009, 20:38:28 pm » |
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Like the choice of fuel delivery
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Stick with what you know works . 13.03 @ 98mph
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jamiep_jamiep
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« Reply #44 on: August 17, 2009, 10:54:50 am » |
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Great to see it running! Always a big thing when you finally get me going I bet your a happy man!
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thehanz DVK
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« Reply #45 on: August 17, 2009, 18:14:10 pm » |
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Like the choice of fuel delivery looks like heineken or bavaria fuel....
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67 bug ragtop 091 berg 5. 2276cc 48 Ida
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mr horsepower
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« Reply #47 on: August 17, 2009, 20:27:36 pm » |
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So today i welded the exhaust pipe to the hairdryer tomorrow it wil be debured grinded sandblased and wraped yes only a few things to do it looks that we be racing in bitburg. wat would you guys think my car could run on the quarter mile? its only a small 1900 wbx gr Henri.
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mr horsepower
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« Reply #49 on: August 25, 2009, 18:44:01 pm » |
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Last monday i got some help from my buddy (tiki madness) we worked on the rollcage and we did some mods on the rear suspention every day we get closer to our goal
THANKS MICHAEL !!!
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« Last Edit: August 25, 2009, 18:52:43 pm by mr horsepower »
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tikimadness
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« Reply #50 on: August 25, 2009, 19:55:38 pm » |
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What the f@#$k was I looking at the holey Mary?
Glad to help you,
Michael
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member of team YAC ; the guys who write history.
GASSER GARAGE a few friends creating history.
NIDGAFWYT
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Shubee2 (DSK)
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« Reply #51 on: August 26, 2009, 00:11:25 am » |
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Like the choice of fuel delivery He is going to need some Running shoes and a Bigger Jug If You plan on using that Fuel Set up LOL
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Der Selten Kafers VW Club. Founding Member Est: 1976
58 Ragtop Old School Cal Look 66 Cal Look Drag Car 67 Resto Cal Look 67 Chevy II Nova L79 02 Camaro Vert! 04 Corvette Vert! 04 Colorado Pickup
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mr horsepower
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« Reply #52 on: October 11, 2009, 13:06:39 pm » |
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So time for an update bitburg didnt went so good for us the thurstday before at 20:15 almost dark i made a testrun drove it of the truck and warmed it up and hit the trottle the turbo spooled up real nice but in a high rpm range due the small 1.9 engine the boost and rpm was not under control i could not read the rpm and boost gauge i was trying to hold the bug on the road it went wel i was thinking bitburg here we come i worked friday to get the car preped for the weekend . at bitburg first run no turbo pressure had no power maybe it was the boost control or rpm limiter . at the second run after checking it blowed a waterplug out of the rear . we worked to get the shit plug watertight it was sitting there for 4 jears and never leaked the thirth run stil no boost and power michael had no more than 3 gears an it woudln shift anymore there was a loose nut at the shifter we maneged to fixed it fourth run i noticed the was a lot of smoke coming out the engine still no power back in the pit there was a cracked intake gasked so i thouged that wher the boost is going we fixed the gasked . fifth run the was a lot of smoke and no power michael called me from the end of the track and told me the oil catch tank was flooding then i knew the race was over . we drove the car back on the truck . but we had a great weekend together with the otto bros and there familly my dad brother racecees tiki madness cnc wizzard delrue micha 64 dirk the four play bad bitch team ome sande and crew and all the other i forgot to write down.
after a week in the garage i pulled the 1\2 head after a cr check there was no cr at at #1cilinder i had loades of under pressure . ill found that piston #1 was cracked between the the cr rings after thinking it over it happend at the test run but the engine sounded verry nice untill the catch tank was full with oil . i mounted a other piston an bolted it back together i went for a test run at saturday and it pulled like crazy on the road wheelspin til third gear everytime exces the 0.5 pressure i drove til 1.0 bar pressure and the car realy kicks ass but in bitburg it was driving like shit
wat i do know is that the tiki turbo set up worked wel and that my engine and transmission is in good shape the car handels good at 180 kmh so the turbo is going on the tiki and my 1.9 gets his supercharger for 2010 season so with a little work the car should perform better next year .
we had a great weekend in bitburg thanks to everyone .
GR Henri.
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« Last Edit: October 11, 2009, 13:29:29 pm by mr horsepower »
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mr horsepower
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« Reply #53 on: October 11, 2009, 13:37:54 pm » |
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h
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tikimadness
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« Reply #54 on: October 11, 2009, 14:53:20 pm » |
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Nice pics of you in fourplay We'll have fun next year Michael
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member of team YAC ; the guys who write history.
GASSER GARAGE a few friends creating history.
NIDGAFWYT
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mr horsepower
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« Reply #55 on: October 11, 2009, 18:38:43 pm » |
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h
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jamiep_jamiep
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« Reply #56 on: October 13, 2009, 10:09:52 am » |
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Sorry to hear of the tough weekend Henri, but at least you have the problem nailed down now.
Great pics too!
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Airspeed
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« Reply #57 on: October 14, 2009, 18:37:37 pm » |
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Ouch, that was a bad case of detonation if you broke two ring lands at once What max boost did you reach too cause this?
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"...these cars were preferred by the racers because the strut front suspension results in far superior handling than the regular torsion bar front end..." - Keith Seume. 10.58 @ 130 mph (2/9/2022 Santa Pod)
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Jesse Wens
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« Reply #58 on: October 14, 2009, 18:41:00 pm » |
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despite the racing it was a great weekend tough. see you next year
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thinking out of the box will get you to go faster cheaper in the long run, time is on my side
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tikimadness
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« Reply #59 on: October 14, 2009, 20:00:37 pm » |
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Ouch, that was a bad case of detonation if you broke two ring lands at once What max boost did you reach too cause this? Around 20 psi @8500 rpm He was so busy trying to keep the car on the road that he didn't notice the high rpm he reached. Michael
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member of team YAC ; the guys who write history.
GASSER GARAGE a few friends creating history.
NIDGAFWYT
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