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Author Topic: The Jägerbug  (Read 14025 times)
peach_
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« Reply #30 on: June 26, 2009, 00:03:52 am »

Sweet Guys looking Really good!
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1966 java green looker- 2276 Street Machine, with standard gear box@ 14.5 (2013), With Pro Street Box @ 13.5 (2014), still more to come!

SAS RENN-WAGENS and proud



#CALLOOKDRAGS
pughdog
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« Reply #31 on: June 26, 2009, 07:54:21 am »

The new rear wheels and slicks should be touching down any day now too from the States Smiley
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AlexB
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Posts: 51


« Reply #32 on: June 27, 2009, 23:23:08 pm »

Quick update:

No longer shredding belts - engine pulling like a train, unfortunately we have a few gearbox issues, seems that we have the gland nut needle bearing is picking up in the input shaft as we have a bit of a lack of synchros on most gears - although if you sit and idle for a while it will go in, pulling the engine tomorrow ( Not a popular choice as its my sons 8th Birthday !) if its the needle bearing then its a simple fix hopefully, failing that its a gearbox swap back to last seasons box for Ebi

We leave weds and we will be ready !!  Grin

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pughdog
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« Reply #33 on: June 27, 2009, 23:47:26 pm »

Amen to that  Wink

I'll be round in the afternoon
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AlexB
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« Reply #34 on: June 28, 2009, 15:01:50 pm »

Ok - engine pulled and culprit found !!



new cush lock disc - lasted 3 ish miles !! although its not its fault - its due to this



secondhand keenedy stage 2 pressure plate which broke one of its springs - one was lodged in with the clutch plate and the other was floating around near the starter - luckily it hadnt got caught up in our new high torque starter!!

So on the phone in the morning to find another clutch pressure and centre plate - hopefully we can get it out in time to fit on tuesday  Shocked
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pughdog
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« Reply #35 on: June 28, 2009, 17:45:26 pm »

 Shocked Team Jägerbug ~ cutting it fine since 2009

 Cheesy
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pughdog
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« Reply #36 on: July 09, 2009, 19:03:14 pm »

Ok, not updated for a while, apologies, we've been very busy!

After grenading the clutch, pressure plate and flywheel dowells just before EBI we were forced to take the Jägerbug with the trusty old 1914 engine to Belgium. The new gearbox stood up to 21 punishing passes and we even managed to better our previous years best times. Partly due to the longer gearing in the new box and the removal of the fanbelt Cheesy

The record now stands at 15.02

Hopefully a time we'll shatter when the new engine makes its debut at BugJam!

So, to cut a very very long story short.... Smiley

We've received the new 4 puck clutch and Kennedy stage 2 pressure plate from SSP (fantastic next day delivery service, thanks Barney Wink ) The new lightened flywheel has also been supplied by SSP and has been fitted using the scat chromoly dowells, hopefully this lot should stay together this time! We've tightened the nut to as high a torque as we could get it on advice from Mr Webb amongst others over in Belgium



The only problem we did experience in Belgium was a difficulty in 3rd gear selection. To sort this we've renewed the shift rod bush and the coupling.



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pughdog
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« Reply #37 on: July 09, 2009, 19:11:05 pm »

I took it out for a test spin today and the gear shifting was much better and crisper. Hopefully it will stand up to the punishment of the new engine!

When I arrived at Alex's he was deep into cutting and sorting out the new exhaust system. We received a prototype 2" stainless header and stinger from a company in the States but it's needed a bit of work to make fit. Here you can see Al tig welding it back together on the engine stand to ensure everthing lines up better



As impressive as the "traffic cone" stinger looked it was decided that it was infact too large and would probably fatigue and snap off unless shortened, a hefty 6 inches were marked up and removed



Out came the grinder!



After working on it for several hours it's now a good fit that looks huge and impressively shiny hanging in place!



Ladies and Gentlemen, we give you the new Jägerbug exhaust system! :eek:

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pughdog
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« Reply #38 on: July 13, 2009, 15:02:42 pm »

Cheers Chris, was good to see you and yours too Wink Hope you managed to get around ok with the sat nav issues et all

Ok, once again ths was the sight in the Jagerbug garage on Friday



Out with the old 1914 engine, 151 quarter mile passes and it's time to let it recover!

in with the new, hopefully the clutch and flywheel will stand up to the job





Once the engine was bolted into place, Alex got on with bolting the carbs etc back on whilst I 'adjusted' the rear valance to clear the new bigger exhaust



Back together pretty quickly and despite a few 'flaming' issues all seems to be running correctly and very very loudly! Cheesy



fingers crossed the slicks arrive in time

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jamiep_jamiep
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« Reply #39 on: July 13, 2009, 16:47:27 pm »

CooL!
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Black Sheep
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less is more


« Reply #40 on: July 13, 2009, 20:54:42 pm »

Looking good lad's , let us know how that new motor gets on this weekend  Cool
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Stick with what you know works .
13.03 @ 98mph
pughdog
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« Reply #41 on: July 14, 2009, 07:32:23 am »

Don't worry, there will be a full report come Monday morning Wink
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AlexB
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« Reply #42 on: July 27, 2009, 11:20:36 am »

OK - heres the pics of stripdown after our rattle at Bugjam

Engine out of car and onto stand



Nothing looks amiss in the rocker box





Head ready to lift off



Looks like the tapping we heard was no4 piston just touching the head



Head -



Barrel off - rod bolts look intact



 :escher:
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AlexB
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« Reply #43 on: July 27, 2009, 11:21:13 am »

OK Piston off, rod removed



Plenty of bearing material around no 4 journal !

No 4 big end shell is toast



Rod shows a bit of heat but measures up in tolerance so hopefully is ok



However the bearing shell is in a very sorry state - some of it on the crank, lots of it in the sump !!



So it looks like we are shopping for a new crank & a full set of engine bearings at least  Sad

Plan for the time being - strip down engine fully and check it over - make sure no shrapnel has done any further damage
remove gearbox from car and strip it down to sort out its selection 'issues' then get the car out and running on its new box with old engine (Again !!) in time for Vw action - at least we will have our new slicks to play with !!  =D
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AlexB
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« Reply #44 on: July 27, 2009, 21:31:11 pm »

Well at last a bit of good news - our slicks and wheels are here !!

Rich collected them from the shippers last friday & i managed to get the slicks fitted this afternoon by shane welton  =D



Nice new shiny Convo Pros



Quick pic of them on the car - they need a good clean yet and some better nut washers machining up but you get the picture



HUGE thanks to Tony at Emu Express for sponsoring these - cannot thank him enough for his support - really looking forward to trying them out on the track !!  =D
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Fasterbrit
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OFF#23 - The Fastest Outlaw in the West!


« Reply #45 on: July 27, 2009, 23:08:17 pm »

Like the new blingin' wheels and tyres Cool Look the nads boys!

Big shame about the motor getting mildly toasted at Bug Jam... still, not as bad as it could have been had that rod let go properly!

Good to catch up with you guys at BJ - diggin' the Jaeger muttonchops Cool matt
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9.563 @ 146.25 mph Cal Look Drag Day, Santa Pod, April 2011
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mr horsepower
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« Reply #46 on: July 28, 2009, 17:52:59 pm »

Hi guys why did that bearing came out of the rod didn t it have any oil did it run dry?
or was there a bearing size failure .

good luck with the rebuild.

gr Henri 
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AlexB
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« Reply #47 on: July 28, 2009, 19:52:13 pm »

Hi guys why did that bearing came out of the rod didn t it have any oil did it run dry?
or was there a bearing size failure .

good luck with the rebuild.

gr Henri 

Hi Henri - really not sure why it let go, its weird as its not the last in line for lube as no 2 rod end is the last so you would expect problems there, it may be a duff bearing or the crank may already have had an issue with that journal - it was a used donated 82mm crank with a .50 grind already, we just measured it up and it appeared in tolerance so we polished the journals and used it !  I will post new pics once we get the bottom end apart and find out what sort of state the main and other rod bearings are in when I return from Spa  Grin
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